Accident | |
---|---|
Date | July 2, 2021 |
Summary | Ditched after engine failure |
Site | Māmala Bay, Oahu 21°16′30″N 158°01′34″W / 21.275°N 158.026°W |
Aircraft | |
Aircraft type | Boeing 737-275C[Note 1] |
Operator | Rhoades Aviation |
Call sign | RHOADES EXPRESS 810 |
Registration | N810TA[1] |
Flight origin | Daniel K. Inouye International Airport |
Destination | Kahului Airport |
Occupants | 2 |
Passengers | 0 |
Crew | 2 |
Fatalities | 0 |
Injuries | 2 |
Survivors | 2 |
Transair Flight 810 was a Boeing 737-200 converted freighter aircraft, owned and operated by Rhoades Aviation under the Transair trade name, on a short cargo flight en route from Honolulu International Airport to Kahului Airport on the neighboring Hawaiian island of Maui on July 2, 2021. Immediately after an early morning takeoff, one of its two Pratt & Whitney JT8D turbofan engines faltered, and the first officer, who was flying the aircraft, reduced power to both engines. The two pilots—the only occupants of the aircraft—began executing the Engine Failure or Shutdown checklist, but became preoccupied with talking to air traffic control (ATC) and performing other flying tasks, never reaching the section of the checklist where the failing engine was to be positively identified and shut down. The captain assumed control but misidentified the failing engine, increased power to that engine, and did not increase power to the other, properly functioning engine. Convinced that neither engine was working properly and unable to maintain altitude with one engine faltering and the other idling, the pilots ditched off the coast of Oahu about 11 minutes into the flight.
The pair were rescued about an hour after the crash in a coordinated inter-agency response involving multiple aircraft and boats. Both were hospitalized and later released. The wreckage was located the following week at depths up to 420 feet (130 m) 2 miles (3 km) off Ewa Beach and was subsequently recovered.
The Federal Aviation Administration (FAA) and National Transportation Safety Board immediately began investigating. Transair voluntarily withdrew its four remaining 737s from service for an internal review. Transair resumed flying their one operational 737-200 a week later, but subsequently had to cease 737 operations due to deficiencies identified by the FAA prior to the ditching. The NTSB report cited the pilots' ineffective crew resource management, high workload, and stress.
Cite error: There are <ref group=Note>
tags on this page, but the references will not show without a {{reflist|group=Note}}
template (see the help page).